Deepwater Horizon Blowout Animation

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Just so people are aware, the Trump administration's proposed budget cuts all CSB (makers of this video) funding. Without this organization there is very limited resources for investigating these accidents and the mistakes of the past will not provide the information needed to improve the safety of the chemical industry. The CSB and regulatory agencies such as OSHA are the reason why the US doesn't experience disasters like Bohpal and that when accidents like these do happen, they only happen once.

👍︎︎ 17 👤︎︎ u/Quinlanofcork 📅︎︎ Sep 20 2017 🗫︎ replies

This is absolutely fascinating, and brings to mind the Swiss Cheese Model. Thank you for sharing!

👍︎︎ 5 👤︎︎ u/wonderplatoon 📅︎︎ Sep 21 2017 🗫︎ replies
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April 20th 2010 11 workers died and 17 were seriously injured by an explosion on the Deepwater Horizon an offshore drilling rig located approximately 50 miles off the coast of Louisiana the rig burned for two days eventually sinking and triggering the largest oil spill in US history as oil and gas spewed up from the seafloor the Deepwater Horizon had been drilling an oil well in 5,000 feet of water in an area of the Gulf of Mexico known as the Macondo prospect in 2010 the CSB launched an investigation to examine the technical organizational and regulatory factors that contributed to the accident during the investigation the CSB made new findings about why a key piece of safety equipment the deepwater horizons blowout preventer failed to seal the well during the emergency these new findings help explain why the accident was so devastating and the CSB cautioned that other blowout preventers currently in use could fail in similar ways drilling an offshore well involves creating a pathway between the drilling rig and oil and gas reservoirs trapped beneath the seafloor a deep hole or well bore is drilled through layers of subsea rock and sediment these rocky layers can contain crap water crude oil and natural gas under pressure an unplanned flow of these well fluids into the well bore known in the industry as a kick can be dangerous without careful management a kick can lead to a blowout the uncontrolled release of flammable oil and gas from the well a blowout can be catastrophic since oil and gas reaching the drilling rate can quickly find an ignition source or explosion endangering the lives of the drilling crew to prevent kicks drillers pompe dents slurry called drilling mud into the well creating a barrier between the undersea oil and gas and the piping that leads to the rig if this mud barrier fails or is somehow removed the safety of the drilling crew depends on a critical piece of equipment located on the sea floor called the blowout preventer or Bo P the Bo P is a complex electrically and hydraulically powered device that is essential for controlling the well and in an emergency situation preventing a disaster on the platform high above on the sea surface the Bo P is connected to the rig by a large diameter pipe called a riser if a kick occurs the blowout preventer is designed to prevent flammable oil and gas from traveling up the riser to the drilling rig this is done by sealing the area around the drill pipe known as the annular space to do this the crew can manually close pipe Rams and donut shaped rubber devices known as annular preventers if those devices should fail to work the last resort is a pair of sharp metal blades which form a blind shear Ram designed to cut the drill pipe and seal the well the blind shear Ram can be activated manually or by automated emergency systems at approximately 8:45 p.m. on April 20th 2010 a kick occurred in the Macondo well oil and gas entered the well bore undetected eventually passing above the blowout preventer and traveling quickly up the riser toward the Deepwater Horizon and the 126 people on just after 9:40 p.m. drilling mud forced upwards by the rising oil and gas suddenly blew out onto the rig crew members responded by closing the upper annular preventer in the Bo P however this did not seal the well as intended and flammable oil and gas continued to flow into the riser toward the rig next the crew closed a pipe Ram this successfully closed the annular space and sealed the well but tragically this proved to be only a temporary fix oil and gas that were already above the pipe Ram continued to flow inexorably toward the Deepwater Horizon at approximately 949 p.m. the flammable hydrocarbons found an ignition source the first explosions shown at the Deepwater Horizon as the oil and gas escaped the riser onto the rig the pressure dropped in the annular space above the pipe Ram but at the same time the pressure in the drill pipe climbed substantially the drill pipe was closed at the top but oil and gas continued to flow in from the reservoir below after extensive analysis the CSB concluded that this large difference in pressure likely caused the drill pipe to buckle essentially bending the pipe off-center inside the blowout preventer the buckling pushed sections of the drill pipe outside of the reach of the blind shear Ram blades this would eventually prove to be catastrophic with the drill pipe buckled the explosion and subsequent loss of electrical and hydraulic power from the raid likely activated an automated system on the blowout preventer known as the AMF Deadman which closes the blind sheer Ram and cuts the drill pipe this emergency system is designed to activate when electric power hydraulic pressure and communications from the rig have been lost the AMF Deadman system was operated by two redundant control systems on the Bo P known as the yellow pod and the blue pod the redundancy is supposed to increase the reliability of the system in an emergency situation the yellow and blue pods worked independently of each other and were comprised of identical enclosed computer systems and sets of solenoid valves when activated the solenoid valves controlled important Bo P functions such as closing the blind shear Ram if electrical power from the rig was lost has happened on April 20th 2010 both the yellow and blue control pods contained backup 27 volt and nine volt batteries to power emergency functions the nine volt batteries powered computers that would activate the solenoid valves which were powered by the 27 volt batteries however evidence indicates the blue pod had been miss wired at some time before the Bo P was lowered onto the sea floor this caused the pods 27 volt battery to drain and made it impossible to operate the solenoid valve for the blind shear Ram on the night of the accident and within the redundant yellow pod the solenoid for the blind shear Ram had been miss wired the solenoid valves were controlled by two coils of electrical wire these two coils were designed to work in concert generating a magnetic field strong enough to operate the valve but within the miswired solenoid valve the two coils actually opposed each other leaving the valve paralyzed only a third unplanned failure allowed the yellow pod to operate on the night of the accident one of the 9-volt batteries that powered the solenoid valves computer had failed as a result the affected computer system could not initiate the command to energize the miswired coil had both coils of the miswired solenoid valve and energized the two coils would have generated opposing forces on the valve the solenoid valve would have remained closed and the blind shear Ram would never have been closed however the failed battery rendered one coil inoperable and most likely allowed the other coil to open the solenoid valve by itself this in turn initiated closure of the blind shear Ram this should have cut the drill pipe and sealed the well greatly reducing the impact of the accident but because the drill pipe was buckled and off-center inside the blowout preventer it was trapped and only partially cut with the failure of this last-ditch measure there was nothing left to stop the massive oil spill and the destruction of the ring during its investigation the CSB identified a mechanism that likely caused the drill pipe to be buckled around the time of the explosion this mechanism is called effective compression although effective compression had previously been noted as a hazard in other drilling operations it had never been identified as a problem affecting drill pipe during well operations effective compression occurs because although pipe may appear to be perfectly straight in fact it has minut bends and irregularities invisible to the naked eye along these bends the side of the pipe that is curved outward is slightly longer and has more surface area than the other side when there is a large difference in pressure between the inside and outside of the pipe has happened on April 20th 2010 the longer side of the pipe experiences a larger bending force eventually this force can become great enough to buckle even heavy pipe this is an important finding CSB investigators said because the same conditions of differential pressure could occur at other drilling rigs even if a crew successfully shuts in a while the CSB warned this could make existing blowout preventer designs less effective in emergency situations in the case of the Deepwater Horizon accident the buckled drill pipe prevented the blind shear Ram from sealing the well oil and gas from the well flowed out of the buckled drill pipe and into the Gulf of Mexico for 87 days a reported 5 million barrels of oil eventually spilled causing one of the worst environmental disasters in United States history [Music] you
Info
Channel: Alertometer
Views: 3,409,523
Rating: 4.8466992 out of 5
Keywords: Accidents Happen (Film), Blowout, accidents, human error
Id: 9NQ8LehUWSE
Channel Id: undefined
Length: 11min 23sec (683 seconds)
Published: Thu Jun 05 2014
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