Repairing a Remington 1900 Double Barrel Shotgun | MidwayUSA Gunsmithing

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I remember that guy! I used to love watching his videos. Thanks for posting!

👍︎︎ 14 👤︎︎ u/lomlslomls 📅︎︎ Apr 27 2020 🗫︎ replies

This was great. I loved how thorough his explanations were. I have an older SxS that has an ejector gone bad as well and now I feel I can repair it myself because he walked me thru the whole process!

👍︎︎ 6 👤︎︎ u/eatgoodneighborhood 📅︎︎ Apr 28 2020 🗫︎ replies

I'm Larry Potterfield, and that's the way it is!

👍︎︎ 4 👤︎︎ u/teaching-man 📅︎︎ Apr 28 2020 🗫︎ replies

Love this channel but the latest ones were barely a minute long. He is so thorough I love them.

👍︎︎ 2 👤︎︎ u/DumbDumbGoodbye 📅︎︎ Apr 28 2020 🗫︎ replies
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This old Remington shotgun has lots of  problems, but they're all repairable,   let me show you how. It's a model 1900  side-by-side made about 1904 and has   seen better days. Collectors refer to this as  a KED grade. The "K" refers to the basic grade,   the "E" indicates it has automatic ejectors, and  the "D" refers to the Damascus barrels, KED grade.   We call this a numbers-matching gun which means  the serial numbers on the barrels receiver forend   and many of the small parts all match. These  guns were hand fit during the manufacturing   process and the serial numbers on the parts kept  them together. During my initial inspection,   I discovered several problems. The forend won't  stay attached, the barrels are off the face,   which means they aren't tight against the  receiver. Also one of the automatic ejectors   doesn't work. It's problems like these that  let you know this gun saw a lot of hard use.   The first problem to fix is the forend latch,  it's a small spring that secures the forend to   the barrels and is referred to as a baker style  latch. Taking the forend off another Remington   1900 it's easy to see how the latch works, pretty  clever idea that was patented in the 1880s. I start by disassembling the forend, the  wood is held to the iron by two screws and   a single cross pin retains the latch. The  pin is driven out with a small punch using   a bench block for support. Since I have an  original latch to copy it functions as a   pattern. I have a piece of 3/16" spring  steel flat stock which closely matches   the thickness of the original latch. First I  need to determine the size of the cross pin   hole. The pin itself is about a hundred  and five-thousandths, a #35 drill is a   hundred and ten thousandths which is just large  enough to let the latch spring rotate freely After coating the steel with dykem, I scribe  the approximate width of the latch spring and   the location of the cross pin hole.  An automatic center punch is used to   mark the location of the hole. After center  drilling, I follow with the #35 drill. Next,   I saw out the rough flat spring. Now it's a pretty  simple matter to file and forge the steel to the   correct shape. I use a 10-inch second cut hand  file to remove the bulk of the material and   establish the correct width. The next step  is to forge the front end a little wider. A torch is used to heat the  metal red-hot and a 24-ounce   hammer provides enough power to upset the metal. After letting it cool, you can see that  we have the basic shape. Now I begin to   file the latch to the correct taper, once this is  established the next step is to shape the curve. I have a small shop maid fixture that  would duplicate the original shape. Heat and careful use of a big hammer  forms the curve. The new latch spring   is still rough and oversized but a bit of  filing will bring it to the final shape. Once all the shaping is complete, I  cut it to the correct length. Then   install the new latch to make sure  it holds the forend iron securely,   it snaps right on. Next I'll polish the  spring with the selection of abrasive paper   finishing with 320 grit. A small file is used as  a backer. All polishing must be done lengthwise,   any marks that go across the spring  may cause it to break at that point The latch still needs to be hardened and  tempered. For hardening, I heat the spring   red-hot then quickly dunk it in quenching oil. Oil  is used rather than water as water will cool the   part too quickly and may cause it to crack.  It's now glass hard so I need to temper it   which will remove some of the brittleness, but  before the spring is tempered I need to remove   the scale created during the hardening process.  It's pretty easy to temper the spring in nitre   bluing salts. The salts are brought to about 600  degrees and the latch submerged, once the steel   turns a nice blue color it's dunked in water.  Now we have a genuine working spring with a   finished look. The finished latch is reinstalled  in the forend iron and the iron snapped back on. With the forend latch complete, the  barrels can now be put back on face.   They should fit tightly against  the face of the breech and have   a slight gap about the thickness  of a piece of paper at the bottom. This William Cashmore double made in England is  a great example. The barrels are tight against   the receiver, and a three-thousandths feeler  gauge will just fit between the bottom of   the barrels and the receiver. The latch was  repaired first as the forend iron needs to   be attached during this process. As you can  see the barrels of this Remington 1900 are   loose. A six-thousandths feeler gauge easily  slides between the barrels and the receiver.   One old gun traders trick is to put a small  piece of paper or business card in the hook. This will temporarily tighten up  the gun but after a few cycles of   opening and closing the barrels will  be loose again. It's something to be   on the lookout for if you're inspecting an  old gun. Another trick is to upset or peen   some metal on the hook. This is a sure sign  of an amateur repair and won't keep the gun   tight for long. There are several correct  ways to put the barrels back on face. On some guns, a new oversized hinge pin can  be installed and the hook on the barrels   fit to the new pin. Another technique is  to weld up the hook and refit it to the   existing hinge pin. In addition, the Brits  used a process called shimming the hook,   in which a piece of steel was dovetailed into  the hook and the barrels refit. I'm going to   use a variation of shimming the hook using a  bit of modern technology. A couple of things   the old-time gunsmith didn't have were modern  adhesives and ultra-thin steel shim stock. I'll   glue the appropriate thickness of shim stock  to the hook using 680 green Loctite. Then   I'll smoke the barrels back in just like  it's been done for over a hundred years. Before starting, I need to true up the face of  the receiver. This gun has a small burr at the   corner which is easily removed with a fine stone.  I also polish the back of the barrels removing   the light pitting, it's important to do this  step first before the barrels are put back on   face. Abrasive paper around a file will do the job  nicely. I'm careful to keep the file flat against   the back of the barrels. I only need to use 400  grit paper as any finer polish would be ruined   when I fit the barrels to the receiver. Once I've  cleaned up the breech ends the barrels and forend   iron are reattached. Even with cleaning up the  breech and polishing the back of the barrels,   the six-thousandths feeler gauge is still  the largest that fits in the gap. I know   the barrels need to be set back at least six  thousandths and a couple extra thousands will   give me enough material to fit the barrels. I  cut a piece of eight-thousandths shim stock just   slightly larger than the hook. Ordinary  scissors easily cut this thin material. Looks pretty good. Now high degreese both  the hook and the shim 680 green Loctite has   a relatively thick consistency and fills  any small gaps. With both surfaces coated   a short piece of half-inch dowel and the clamp  hold the shim tight against the hook until the   Loctite cures. Once the Loctite is cured, the  excess shim stock is dressed down even with the   hook. Notice I've removed the extractors they  should be out when fitting the barrels. smoke   from a small lamp will show how much contact  there is between the hook and the hinge pin. We have almost full-contact. Smoke on  the back of the barrels will show where   they are touching the receiver. Now when  I put the barrels on and try to close the   action I can see metal will have to be  removed for the gun to close completely. Using a needle file I carefully remove the high  spots. These are indicated by shiny areas where   the smoke has rubbed off. The process of smoking  and filing is repeated. After a few cycles,   the barrels are making more contact but the top  lever is still well right-of-center. The gap at   the water table is about seventeen-thousandths,  so plenty of travel remains to bring the barrels   down and allow the lever to move closer  to center. A bit more work and the barrels   fit tight against the receiver and I  have a small gap at the water table,   now the barrels are back on face. All of the  file marks are polished out starting with 220   grit abrasive paper and finishing with 400. The  extractors are reinstalled and I make sure the   gun closes with them in place. The last item  on the repair list is one of the automatic   ejectors. Their purpose is to automatically  eject empty shells when the gun is open. The extractors are located in the barrels and  are hit by the ejector hammers in the forend,   which are powered by small v-springs. In this  case, the right ejector needs to be repaired.   I remove the broken spring during my initial  inspection, all the pieces are here so I've   got a pattern to work from. This piece of spring  stock closely matches the thickness of the ejector   spring. The first step is to bend the metal over  double to form the two legs of the spring. Using   a torch I heat it red hot and bend at the mark.  The steel should be allowed to cool naturally as   cooling it in water would harden it making shaping  difficult. The ejector spring is only about a   hundred and seventy-thousandths wide, so I'll have  to cut the spring stock down to match the width.   It's a simple matter to mark the new spring for  the correct width and file to the line. Now I need   to taper the legs the first leg needs to taper  from about fifth-thousandths, all the way to the   full thickness of the spring stock. It also tapers  in width down to about 125 thousandths. The second   leg is formed the same way. However, there's a  little foot on the end that has to be filed in.   Keeping the spring attached to the long piece of  stock, makes holding it in the vise much easier.   An 8-inch file makes quick work of it. With the  legs tapered and shaped, I cut off the spring.   Now we can bend the legs of the spring to match  the original and polish out all of the file marks.   Here comes the fun part. The spring is heated  red-hot and quickly dunked in quenching oil,   at this point it's glass hard. I need to temper  it which will allow it to flex and return to its   original shape without breaking. First I remove  all of the scale from hardening, the nitre bluing   salts are heated to about 600 degrees, and the  spring immersed. Once the steel turns a nice   blue color it's dunked in water. I compress it  in a vise to make sure that I have a spring.   Now it can be installed in the forend iron and the  forend reattached. once the gun is back together I test it with some dummy rounds, works like new.
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Views: 3,065,032
Rating: 4.8239274 out of 5
Keywords: midwayusa, larry potterfield, midway, gunsmithing, remington, remington 1900, double barrel shotgun, shotgun, repair, gunsmith, back to face, ejector spring, tighten action
Id: O_gI3WX6Uww
Channel Id: undefined
Length: 16min 42sec (1002 seconds)
Published: Wed Jan 08 2014
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